Resources

Consult our range of free resources.

Contact Us

Technical Guides

Tetra has published a series of guides which are available for ordering.

HRSG Inspection Planning Guide (2nd Edition)

Inspection is part of routine maintenance for any Heat Recovery Steam Generator (HRSG). Visual inspections are performed at regular intervals in accordance with the requirements of regulatory bodies and insurers.

HRSG Tube Failure Diagnostic Guide (3rd Edition)

Heat Recovery Steam Generator (HRSG) tubes provide the media for extraction of useful energy from the waste heat in gas turbine exhaust at combined cycle power plants (GT-CCs) or from heat generated by process streams at petrochemical facilities.

Technical White Papers

A selection of technical papers available for reference.

Thank you! Your submission has been received!
Oops! Something went wrong while submitting the form.
Piping Hangers & Supports

Piping Hangers & Supports

Piping supports and hangers require routine inspection. Interferences with equipment or structures can c...

learn more
Reasons for Inspecting

Reasons for Inspecting

Inspection is part of routine maintenance for any Heat Recovery Steam Generator (HRSG). Visual inspectio...

learn more
Grade 91 Steel

Grade 91 Steel

Background Early failures of components fabricated with Creep Strength Enhanced Ferritic (CSEF) Steels in con...

learn more
Flow Accelerated Corrosion (FAC)

Flow Accelerated Corrosion (FAC)

Background Tube thinning caused by flow-accelerated corrosion (FAC) is one of the most frequent causes of fai...

learn more
Duct Burners

Duct Burners

Excess air in the gas turbine exhaust allows the combustion of additional fuel via supplemental firing in the ...

learn more
HRSG Tube Failure Diagnosis

HRSG Tube Failure Diagnosis

Diagnosis of HRSG tube failure causes is not always straightforward. Sometimes, a relatively clear-cut c...

learn more

Contact Us

To discuss how we might assist you to improve your plant's performance or to maintain its value over time

Contact Us

Papers, Presentations and Articles

Selected papers, presentations and articles from major industry conferences and events.

Title
Author
What do HRSG tube failure statistics tell us?
What do HRSG tube failure statistics tell us?What do HRSG tube failure statistics tell us?
Misha Gadher & Mark Taylor
Modern Power Systems
Counterfeit, Fraudulent and Suspect Items (CFSI) – Steel and HRSGs
Counterfeit, Fraudulent and Suspect Items (CFSI) – Steel and HRSGsCounterfeit, Fraudulent and Suspect Items (CFSI) – Steel and HRSGs
Taylor M.
IMechE HRSG User Group 2022
Adapting Existing Thermal Desalination Plants to Produce Hydrogen
Adapting Existing Thermal Desalination Plants to Produce HydrogenAdapting Existing Thermal Desalination Plants to Produce Hydrogen
Malloy J.
2022 World Utilities Congress
Root Cause Failure Investigation of MSCV Drain Failures
Root Cause Failure Investigation of MSCV Drain FailuresRoot Cause Failure Investigation of MSCV Drain Failures
P. Jackson, A. Wholey, E. Tsai and D. Burns
ASME 2022 Pressure Vessels & Piping Conference
Predicting and Preventing Risk of Vibration Induced Failures in Boilers and Heat Recovery Steam Generators (HRSG)
Predicting and Preventing Risk of Vibration Induced Failures in Boilers and Heat Recovery Steam Generators (HRSG)Predicting and Preventing Risk of Vibration Induced Failures in Boilers and Heat Recovery Steam Generators (HRSG)
Fabricius A., Malloy J., Taylor M., Moelling D.
Proceedings of the ASME 2022 Power Conference

Previous Projects

With over 30 years of experience in power and industrial steam generation services, Tetra Engineering has along history of projects.

Root Cause Analysis of HP Drum Nozzle Cracking, 2018
Europe

Root Cause Analysis of HP Drum Nozzle Cracking, 2018

During the 2018 shutdown at a CCGT in Europe several of the HRSG HP drum riser nozzle and downcomer nozzle welds were checked and all were found to be cracked on the inside of the drum, at the weld toe or between weld beads, with the cracks following the fusion line back to the nozzle. The drum feedwater inlet and steam outlet nozzles (above drum waterline) were both undamaged. The drums were removed and all welds were repaired in the workshops. Tetra performed Finite Element Analysis (FEA) and operational data analysis and could conclude that the operational stresses were high enough given the current cycling regime to cause the cracking observed. The quality and design of the original welds is also likely to have contributed to the cracking.

Diverter Damper Design & Operation Review, 2018
Middle East

Diverter Damper Design & Operation Review, 2018

Tetra was engaged by a client to investigate the recently observed cracking on the diverter damper actuator. The design documentation and failure mode was reviewed. From this initial review it could be concluded that the shaft cracking is most likely a result of the operating procedure, where  the damper is kept in an open position for an extended period of time. The exposure to hot flue gas in combination with the load acting on the toggle arms is the most likely source of the cracking

Flow Accelerated Corrosion Risk Assessment, 2017
South East Asia

Flow Accelerated Corrosion Risk Assessment, 2017

An assessment of the susceptibility of HRSG piping components was performed according to Tetra Engineering’s FACRisk™ methodology which includes the use of thermal modelling simulation software (PPSD). From each system, sub groups are ranked using both time to minimum wall thickness and wear rate. The highest risk components (such as elbows, tees and valves) are identified. Overall, due to relatively high operating pH level (>9.2), the overall risk of FAC failures at the CCGT plant in question was considered to be relatively low, with few specific areas showing increased risk. Three separate load cases were simulated and analysed to determine the potential FAC risk. The results of each simulation were incorporated into the final locations recommended for inspection.

Boiler Tube Failure Root Cause Analysis, 2017
Asia

Boiler Tube Failure Root Cause Analysis, 2017

After several tube failures in recent years in the 1st row of LTRH hanger tubes, Tetra was tasked with performing a Root Cause Analysis (RCA) to determine the underlying cause of the failures. A detailed review of operating data, failure reports and design information was carried out and potential causes investigated. The tube failure mechanism as determined by metallurgy was short-term overheating, with temperatures likely exceeding 700°C prior to failures. Two contributing causes were identified by elimination of all other possibilities: temporary loss of steam flow in affected leading row tubes coupled with high flue gas temperatures in certain tubes at the side of the boiler gas path.  Unfortunately, the underlying root cause of the loss of flow could not be confirmed, whereas the asymmetric flue gas temperature distribution is a known issue since commissioning.

Contact Us

To discuss how we might assist you to improve your plant's performance or to maintain its value over time

Contact Us